Evaluation of factors responsible for high effluent suspended solids events in the Kuwahee wastewater treatment plant
Abstract (Summary)
The potential factors causing high effluent suspended solids (ESS) in Kuwahee
Wastewater Treatment Plant (WWTP) are studied in order to properly identify the reason
or reasons that might lead to focus future studies in proper remedial actions in the facility.
In this document an analysis protocol is established, and several factors are evaluated for
potential associations with high ESS events. From the protocol some of the factors were
collected from regular operational procedure and others were collected during a study
sampling period.
The analysis of those factors included in the protocol showed no biological, or
hydraulic, or settling parameters causing the suspended solids content to rise in the plant
effluent. However, some flow distribution problems were found when the inflow to each
clarifier was sampled and evaluated. This leaded to clarifier differences in performance
that were corrected during the study period, after adjusting the flow openings to each
clarifier.
One of the most important evaluations carried out during the analysis, showed
that the average suspended solid concentration taken at the effluent weir of the secondary
clarifiers was smaller than the average ESS concentration taken at the overall plant
effluent. This suggests the presence of another source of suspended solids contributing to
the final ESS at the plant discharge flow.
As part of the sampling procedure DSS/FSS testing was carried out on selected
clarifiers. The clarifiers sampled during the sampling period were different from each
other. The results showed that those clarifiers with flocculation well had a better
performance than the one that has a conventional center well. However, the final
statement could not be related for sure to the better performance of the flocculator
clarifiers due to operational differences.
In Kuwahee WWTP a secondary diversion is used when the inflow exceeds the
maximum hydraulic capacity of the biological reactor. Since the diversion carries the
flow from the primary clarifier effluent to the chlorination basin influent, it was thought
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to be one of the sources of high suspended solids events. In that, a simulation of different
flows was run, in order to understand the incidence of the bypass in the final suspended
solids concentration. The simulation showed that during bypass mode (secondary
diversion is open) the overall plant ESS concentration increases with increasing diverted
flow. Further study is suggested, along with possible solutions to high ESS problems.
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Bibliographical Information:
Advisor:
School:The University of Tennessee at Chattanooga
School Location:USA - Tennessee
Source Type:Master's Thesis
Keywords:water treatment plants tennessee
ISBN:
Date of Publication: