Development of a struvite crystallizer for reducing phosphorus in effluent from livestock waste lagoons
Abstract (Summary)
BOWERS, KEITH EDISON. Development of a Struvite Crystallizer for Reducing Phosphorus in
Effluent from Livestock Waste Lagoons. (Under the Direction of Philip W. Westerman.)
The research successfully met its objectives of designing and characterizing a crystallizer for
removing phosphorus from livestock lagoon effluent in North Carolina. A design was created for a
struvite crystallizer utilizing a cone-shaped continuous-mode fluidized bed. A laboratory-scale
system operating at 49.2 L/h of total liquid flow achieved near-steady state operation at two sets of
operating conditions. The first used ammonia addition of 100 ppm and no magnesium (Mg) addition.
The second used ammonia addition of 100 ppm and Mg addition of 30 ppm. Estimated reduction in
orthophosphate phosphorus (OP) and total phosphorus (TP) was 36% and 24%, respectively, over the
first condition set and 74% and 58%, respectively, over the second. Three models were developed to
describe crystallizer behavior. The MLMB model assumed perfect mixing of both liquid and bed.
The PLCB model assumed plug flow of liquid and perfect classification of the bed. The PLMB
model, which best predicted behavior, assumed plug flow of liquid and perfect mixing of the bed.
Factorial experiments were conducted to test the effects of Mg addition, ammonia addition, and flow
rate on phosphorus removal. Increasing Mg addition in the range tested (0 to 60 ppm) and increasing
ammonia addition in the range tested (0 to 200 ppm) were significantly associated with increasing
phosphorus removal. The effect of flow rate was insignificant between the values tested (41.2 and
56.8 L/h). A field-scale system was assembled at a lagoon and used to conduct factorial experiments
testing the same effects as those in the laboratory. Increasing Mg addition in the range tested (0 to 60
ppm), increasing ammonia addition in the range tested (from no pH enhancement to 1 pH point
enhancement), and decreasing flow rate between the values tested (341 and 568 L/h) were all
significantly associated with increasing phosphorus removal. Reduction in TP and OP averaged
70.2% and 77.3%, respectively, when ammonia and Mg were being added. Peak reductions in TP
and OP were 81.9% and 87.1%, respectively.
Bibliographical Information:
Advisor:
School:North Carolina State University
School Location:USA - North Carolina
Source Type:Master's Thesis
Keywords:north carolina state university
ISBN:
Date of Publication: